Team Solution Prevented Equipment Pull and Saved Operator USD ...

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CASE HISTORY

Team Solution Prevented Equipment Pull and Saved Operator USD 600,000 Location: Canada

Results Saved

operator USD 600,000 since equipment pull was avoided

Baker

Hughes knowledge and experience led to a system solution

Challenges Canadian

operator installed ESP system from Baker Hughes but experienced unstable operation

System

had problems with current fluctuations and underloading

Operator

approached Baker Hughes for a solution before pulling equipment and spending USD 600,000 for competitor’s ESP system

An operator in Canada installed a Baker Hughes electrical submersible pumping (ESP) system. From the beginning, the system was unstable and struggled with current fluctuations and underloading. Production had an erratic range of from 1,056 to 2,264 BFPD (168 to 360 m3/day). After running tests and diagnostics, the operator considered a system pull and replacement using a competitor’s ESP equipment. However, hesitant to spend USD 600,000 for a competitor’s system replacement, the operator approached Baker Hughes for a solution. The account manager studied the installation and suggested changing the direction of the pump’s operation. A Baker Hughes engineeringsupport team agreed after studying the system’s trending data. This data showed that the pump appeared to be functioning in a backward pattern. Further investigation revealed that the operator had initially installed the pump without proper rotation check as a result of production spiking-up on either direction.

Production

had erratic range of from 1,056 to 2,264 BFPD (168 to 360 m3/day)

Baker Hughes solution Account

manager suggested changing pump’s operating direction

ESP system from Baker Hughes delivers valuable trending data for operator.

Engineering

After the system’s pump rotation was changed, production immediately increased and stabilized. Wear decreased, uptime improved, and production increased 43%. Because the Baker Hughes accounting manager and the engineering support team were able to diagnose and solve the installation problem, the operator gained a fix for the recurring problem; ongoing operational improvements; and savings of USD 600,000 by avoiding an equipment pull.

Operator

support detected trend showing what appeared to be backward pump operation changed pump rotation and production increased

Proper

rotation and increased steam led to stable production

Production

increased 43% to 3,170 BFPD (504 m3/d)

Wear

and tear decreased, which improved run life

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© 2013 Baker Hughes Incorporated. All rights reserved. 38987 11/2013